故障代码 | 故障现象/类型 | 故障原因 | 解决对策 |
1 | Overcurrent | Short circuit/earth fault at the output. Motor too large. Faulty output stage. | Remove short-circuit. Connect smaller motor. If fault can still not be reset, contact SEW service. |
2 | DC link voltage | DC link voltage too high. | Increase deceleration ramps. |
3 | Brake chopper | Regenerative power too high Braking resistor circuit interrupted Short-circuit in the braking resistor circuit Braking resistance value too high Faulty brake chopper | Increase deceleration ramps. Check connecting leads of the braking resistor. Check technical data of the braking resistor. Exchange MOVITRAC® 31C |
5 | Regenerative overload | With active regen. n monit. (P520/P522) and speed control (P770): faulty encoder signals wrong number of pole pairs (P324/P344) value of increments (P773) not correct | Check encoder. Check encoder connection. Set number of pole pairs correctly. Set value of increments correctly. |
4 | Cont. overload | ´t utilization too high (> 125(%)). | Reduce load. |
6 | Overtemperature | Thermal overload of the inverter. | Reduce load and / or ensure adequate cooling. |
7 | Phase failure | With active mains volt. monitor.(P530) Phase missing at TL. X1:1/2/3. | Check mains supply. |
10 | Direction of rotation | Only with active speed control (P770): Encoder tracks A/A and B/B are swapped in pairs. Motor rotates in opposite direction. Regen. overload (i.e. with sagging hoist) because of excessive load or BOOST setting too low (P321/P341). | Check encoder connection. Exchanging two motor phases. Reduce load or increase BOOST. |
11 | Speed detection | Only with active speed control (P770): Faulty encoder connection. FEN31C/FPI31C option not installed. | Check encoder connection. Insert correct option (FEN31C or FPI31C). |
12 | Mot. overload | With active n monit. (P510/P512) and speed control (P770): faulty encoder signals wrong number of pole pairs (P324/P344) value of increments (P773) not correct | Check encoder. Check encoder connection. Set number of pole pairs correctly. Set value of increments correctly. |
13 | Starting conditions | With active hoist function (P710/P712): Current too low during the premagnetization phase: Motor rated power selected too small in relation to the inverter rated power. Cross-section of the motor leads too small. | Check startup data and carry out new startup if necessary. Check inverter-motor connection. Check cross-section of the motor leads and increase if necessary. |
14 | Output open | With active hoist function (P710/P712): Two or all output phases interrupted. Motor rated power selected too small in relation to the inverter rated power. | Check inverter-motor connection. Check startup data and carry out new startup if necessary. |
17 | Stack overflow | Inverter electronics faulty. Possible cause: EMC effect. | The notes for EMC compliant installation must be observed. The reset for error 25 consists of several steps: 1. Factory setting (P830 = YES) 2. Re-set matched parameters 3. Carry out reset If fault occurs repeatedly, contact SEW service. |
18 | Stack underflow | Inverter electronics faulty. Possible cause: EMC effect. | The notes for EMC compliant installation must be observed. The reset for error 25 consists of several steps: 1. Factory setting (P830 = YES) 2. Re-set matched parameters 3. Carry out reset If fault occurs repeatedly, contact SEW service. |
19 | NMI trap | Inverter electronics faulty. Possible cause: EMC effect. | The notes for EMC compliant installation must be observed. The reset for error 25 consists of several steps: 1. Factory setting (P830 = YES) 2. Re-set matched parameters 3. Carry out reset If fault occurs repeatedly, contact SEW service. |
20 | Undefined opcode | Inverter electronics faulty. Possible cause: EMC effect. | The notes for EMC compliant installation must be observed. The reset for error 25 consists of several steps: 1. Factory setting (P830 = YES) 2. Re-set matched parameters 3. Carry out reset If fault occurs repeatedly, contact SEW service. |
21 | Protected instr. | Inverter electronics faulty. Possible cause: EMC effect. | The notes for EMC compliant installation must be observed. The reset for error 25 consists of several steps: 1. Factory setting (P830 = YES) 2. Re-set matched parameters 3. Carry out reset If fault occurs repeatedly, contact SEW service. |
22 | Word op. access | Inverter electronics faulty. Possible cause: EMC effect. | The notes for EMC compliant installation must be observed. The reset for error 25 consists of several steps: 1. Factory setting (P830 = YES) 2. Re-set matched parameters 3. Carry out reset If fault occurs repeatedly, contact SEW service. |
23 | nstruct. access | Inverter electronics faulty. Possible cause: EMC effect. | The notes for EMC compliant installation must be observed. The reset for error 25 consists of several steps: 1. Factory setting (P830 = YES) 2. Re-set matched parameters 3. Carry out reset If fault occurs repeatedly, |
24 | Ext. bus access | Inverter electronics faulty. Possible cause: EMC effect. | The notes for EMC compliant installation must be observed. The reset for error 25 consists of several steps: 1. Factory setting (P830 = YES) 2. Re-set matched parameters 3. Carry out reset If fault occurs repeatedly, contact SEW service. |